Beware the Cheap Fix: You May Get What You Pay For

Fossil plant required an emergency rebuild when poor quality repair caused a holiday shutdown. 

Written by: Dr. Gary Dyson & Mohamed Mohamed
Published by: Pumps & Systems

The consequences of poor quality repairs can result in premature failure, unplanned outages and higher repair costs because follow up after the initial attempt is considered an emergency repair. That was the situation when a major fossil plant experienced an emergency failure of a six-stage, boiler feed pump element. It was a quiet holiday night when the pump had to be pulled due to lack of flow, causing a plant shutdown. Unfortunately, when the plant tried to set the spare element up on bearings, employees were unable to turn the rotor. In this case, the emergency occurred when the repaired spare element had to be used immediately after initial failure. Thus, the problems with the previous repairs were uncovered.

Because it was the holiday season, the plant’s usual service provider could not respond in the required time. Another Hydro was called in to assess the problem, engineer a solution and save the plant thousands of dollars in downtime.

Field service was mobilized to provide labor in two 24-hour shifts.

Worthington element

Image 1. Worthington element set on precision v-blocks, checking vertical and horizontal clearances at the suction end and discharge end. These checks are used to see if element is concentric.

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Pump Renovation Restores Balance

Vibration issues with a two-stage pump forced a major steel manufacturer to remove the pump from service. Due to incorrect weights welded on an impeller, a steel manufacturer called upon Hydro to repair and balance a two-stage pump.

Written by: Ken Babusiak (Hydro, Inc.)
Published by: World Pumps

The pump was experiencing the vibration during the spring and summer months of 2016. The steel company sent the pump to HydroAire’s Chicago, IL facility in September of that year. HydroAire was able to determine the cause of the vibration and created a solution that got the pump back in operating condition. The pump was installed and back in service by February, 2017.

The initial testing and analysis deter-mined that the impeller had large weights welded onto it. The steel company was concerned for many reasons, especially because the staff knew that using weights was not the correct way to balance an impeller. This caused the steel manufacturer to question the manner in which the pump had previously been repaired.

Weights added to impellers

Adding weights to impellers is generally not standard practice.

Where not to position the weights.

Where not to position the weights.

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